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CVSS v3.1 |
In the Linux kernel, the following vulnerability has been resolved:
bnxt_en: Fix memory corruption when FW resources change during ifdown
bnxt_set_dflt_rings() assumes that it is always called before any TC has
been created. So it doesn't take bp->num_tc into account and assumes
that it is always 0 or 1.
In the FW resource or capability change scenario, the FW will return
flags in bnxt_hwrm_if_change() that will cause the driver to
reinitialize and call bnxt_cancel_reservations(). This will lead to
bnxt_init_dflt_ring_mode() calling bnxt_set_dflt_rings() and bp->num_tc
may be greater than 1. This will cause bp->tx_ring[] to be sized too
small and cause memory corruption in bnxt_alloc_cp_rings().
Fix it by properly scaling the TX rings by bp->num_tc in the code
paths mentioned above. Add 2 helper functions to determine
bp->tx_nr_rings and bp->tx_nr_rings_per_tc. |
In the Linux kernel, the following vulnerability has been resolved:
HID: intel-thc-hid: intel-quicki2c: Fix ACPI dsd ICRS/ISUB length
The QuickI2C ACPI _DSD methods return ICRS and ISUB data with a
trailing byte, making the actual length is one more byte than the
structs defined.
It caused stack-out-of-bounds and kernel crash:
kernel: BUG: KASAN: stack-out-of-bounds in quicki2c_acpi_get_dsd_property.constprop.0+0x111/0x1b0 [intel_quicki2c]
kernel: Write of size 12 at addr ffff888106d1f900 by task kworker/u33:2/75
kernel:
kernel: CPU: 3 UID: 0 PID: 75 Comm: kworker/u33:2 Not tainted 6.16.0+ #3 PREEMPT(voluntary)
kernel: Workqueue: async async_run_entry_fn
kernel: Call Trace:
kernel: <TASK>
kernel: dump_stack_lvl+0x76/0xa0
kernel: print_report+0xd1/0x660
kernel: ? __pfx__raw_spin_lock_irqsave+0x10/0x10
kernel: ? __kasan_slab_free+0x5d/0x80
kernel: ? kasan_addr_to_slab+0xd/0xb0
kernel: kasan_report+0xe1/0x120
kernel: ? quicki2c_acpi_get_dsd_property.constprop.0+0x111/0x1b0 [intel_quicki2c]
kernel: ? quicki2c_acpi_get_dsd_property.constprop.0+0x111/0x1b0 [intel_quicki2c]
kernel: kasan_check_range+0x11c/0x200
kernel: __asan_memcpy+0x3b/0x80
kernel: quicki2c_acpi_get_dsd_property.constprop.0+0x111/0x1b0 [intel_quicki2c]
kernel: ? __pfx_quicki2c_acpi_get_dsd_property.constprop.0+0x10/0x10 [intel_quicki2c]
kernel: quicki2c_get_acpi_resources+0x237/0x730 [intel_quicki2c]
[...]
kernel: </TASK>
kernel:
kernel: The buggy address belongs to stack of task kworker/u33:2/75
kernel: and is located at offset 48 in frame:
kernel: quicki2c_get_acpi_resources+0x0/0x730 [intel_quicki2c]
kernel:
kernel: This frame has 3 objects:
kernel: [32, 36) 'hid_desc_addr'
kernel: [48, 59) 'i2c_param'
kernel: [80, 224) 'i2c_config'
ACPI DSD methods return:
\_SB.PC00.THC0.ICRS Buffer 000000003fdc947b 001 Len 0C = 0A 00 80 1A 06 00 00 00 00 00 00 00
\_SB.PC00.THC0.ISUB Buffer 00000000f2fcbdc4 001 Len 91 = 00 00 00 00 00 00 00 00 00 00 00 00
Adding reserved padding to quicki2c_subip_acpi_parameter/config. |
In the Linux kernel, the following vulnerability has been resolved:
efivarfs: Fix slab-out-of-bounds in efivarfs_d_compare
Observed on kernel 6.6 (present on master as well):
BUG: KASAN: slab-out-of-bounds in memcmp+0x98/0xd0
Call trace:
kasan_check_range+0xe8/0x190
__asan_loadN+0x1c/0x28
memcmp+0x98/0xd0
efivarfs_d_compare+0x68/0xd8
__d_lookup_rcu_op_compare+0x178/0x218
__d_lookup_rcu+0x1f8/0x228
d_alloc_parallel+0x150/0x648
lookup_open.isra.0+0x5f0/0x8d0
open_last_lookups+0x264/0x828
path_openat+0x130/0x3f8
do_filp_open+0x114/0x248
do_sys_openat2+0x340/0x3c0
__arm64_sys_openat+0x120/0x1a0
If dentry->d_name.len < EFI_VARIABLE_GUID_LEN , 'guid' can become
negative, leadings to oob. The issue can be triggered by parallel
lookups using invalid filename:
T1 T2
lookup_open
->lookup
simple_lookup
d_add
// invalid dentry is added to hash list
lookup_open
d_alloc_parallel
__d_lookup_rcu
__d_lookup_rcu_op_compare
hlist_bl_for_each_entry_rcu
// invalid dentry can be retrieved
->d_compare
efivarfs_d_compare
// oob
Fix it by checking 'guid' before cmp. |
In the Linux kernel, the following vulnerability has been resolved:
ice: fix NULL pointer dereference in ice_unplug_aux_dev() on reset
Issuing a reset when the driver is loaded without RDMA support, will
results in a crash as it attempts to remove RDMA's non-existent auxbus
device:
echo 1 > /sys/class/net/<if>/device/reset
BUG: kernel NULL pointer dereference, address: 0000000000000008
...
RIP: 0010:ice_unplug_aux_dev+0x29/0x70 [ice]
...
Call Trace:
<TASK>
ice_prepare_for_reset+0x77/0x260 [ice]
pci_dev_save_and_disable+0x2c/0x70
pci_reset_function+0x88/0x130
reset_store+0x5a/0xa0
kernfs_fop_write_iter+0x15e/0x210
vfs_write+0x273/0x520
ksys_write+0x6b/0xe0
do_syscall_64+0x79/0x3b0
entry_SYSCALL_64_after_hwframe+0x76/0x7e
ice_unplug_aux_dev() checks pf->cdev_info->adev for NULL pointer, but
pf->cdev_info will also be NULL, leading to the deref in the trace above.
Introduce a flag to be set when the creation of the auxbus device is
successful, to avoid multiple NULL pointer checks in ice_unplug_aux_dev(). |
In the Linux kernel, the following vulnerability has been resolved:
fs/smb: Fix inconsistent refcnt update
A possible inconsistent update of refcount was identified in `smb2_compound_op`.
Such inconsistent update could lead to possible resource leaks.
Why it is a possible bug:
1. In the comment section of the function, it clearly states that the
reference to `cfile` should be dropped after calling this function.
2. Every control flow path would check and drop the reference to
`cfile`, except the patched one.
3. Existing callers would not handle refcount update of `cfile` if
-ENOMEM is returned.
To fix the bug, an extra goto label "out" is added, to make sure that the
cleanup logic would always be respected. As the problem is caused by the
allocation failure of `vars`, the cleanup logic between label "finished"
and "out" can be safely ignored. According to the definition of function
`is_replayable_error`, the error code of "-ENOMEM" is not recoverable.
Therefore, the replay logic also gets ignored. |
In the Linux kernel, the following vulnerability has been resolved:
ftrace: Fix potential warning in trace_printk_seq during ftrace_dump
When calling ftrace_dump_one() concurrently with reading trace_pipe,
a WARN_ON_ONCE() in trace_printk_seq() can be triggered due to a race
condition.
The issue occurs because:
CPU0 (ftrace_dump) CPU1 (reader)
echo z > /proc/sysrq-trigger
!trace_empty(&iter)
trace_iterator_reset(&iter) <- len = size = 0
cat /sys/kernel/tracing/trace_pipe
trace_find_next_entry_inc(&iter)
__find_next_entry
ring_buffer_empty_cpu <- all empty
return NULL
trace_printk_seq(&iter.seq)
WARN_ON_ONCE(s->seq.len >= s->seq.size)
In the context between trace_empty() and trace_find_next_entry_inc()
during ftrace_dump, the ring buffer data was consumed by other readers.
This caused trace_find_next_entry_inc to return NULL, failing to populate
`iter.seq`. At this point, due to the prior trace_iterator_reset, both
`iter.seq.len` and `iter.seq.size` were set to 0. Since they are equal,
the WARN_ON_ONCE condition is triggered.
Move the trace_printk_seq() into the if block that checks to make sure the
return value of trace_find_next_entry_inc() is non-NULL in
ftrace_dump_one(), ensuring the 'iter.seq' is properly populated before
subsequent operations. |
In the Linux kernel, the following vulnerability has been resolved:
lwt: Fix return values of BPF xmit ops
BPF encap ops can return different types of positive values, such like
NET_RX_DROP, NET_XMIT_CN, NETDEV_TX_BUSY, and so on, from function
skb_do_redirect and bpf_lwt_xmit_reroute. At the xmit hook, such return
values would be treated implicitly as LWTUNNEL_XMIT_CONTINUE in
ip(6)_finish_output2. When this happens, skbs that have been freed would
continue to the neighbor subsystem, causing use-after-free bug and
kernel crashes.
To fix the incorrect behavior, skb_do_redirect return values can be
simply discarded, the same as tc-egress behavior. On the other hand,
bpf_lwt_xmit_reroute returns useful errors to local senders, e.g. PMTU
information. Thus convert its return values to avoid the conflict with
LWTUNNEL_XMIT_CONTINUE. |
In the Linux kernel, the following vulnerability has been resolved:
can: bcm: bcm_tx_setup(): fix KMSAN uninit-value in vfs_write
Syzkaller reported the following issue:
=====================================================
BUG: KMSAN: uninit-value in aio_rw_done fs/aio.c:1520 [inline]
BUG: KMSAN: uninit-value in aio_write+0x899/0x950 fs/aio.c:1600
aio_rw_done fs/aio.c:1520 [inline]
aio_write+0x899/0x950 fs/aio.c:1600
io_submit_one+0x1d1c/0x3bf0 fs/aio.c:2019
__do_sys_io_submit fs/aio.c:2078 [inline]
__se_sys_io_submit+0x293/0x770 fs/aio.c:2048
__x64_sys_io_submit+0x92/0xd0 fs/aio.c:2048
do_syscall_x64 arch/x86/entry/common.c:50 [inline]
do_syscall_64+0x3d/0xb0 arch/x86/entry/common.c:80
entry_SYSCALL_64_after_hwframe+0x63/0xcd
Uninit was created at:
slab_post_alloc_hook mm/slab.h:766 [inline]
slab_alloc_node mm/slub.c:3452 [inline]
__kmem_cache_alloc_node+0x71f/0xce0 mm/slub.c:3491
__do_kmalloc_node mm/slab_common.c:967 [inline]
__kmalloc+0x11d/0x3b0 mm/slab_common.c:981
kmalloc_array include/linux/slab.h:636 [inline]
bcm_tx_setup+0x80e/0x29d0 net/can/bcm.c:930
bcm_sendmsg+0x3a2/0xce0 net/can/bcm.c:1351
sock_sendmsg_nosec net/socket.c:714 [inline]
sock_sendmsg net/socket.c:734 [inline]
sock_write_iter+0x495/0x5e0 net/socket.c:1108
call_write_iter include/linux/fs.h:2189 [inline]
aio_write+0x63a/0x950 fs/aio.c:1600
io_submit_one+0x1d1c/0x3bf0 fs/aio.c:2019
__do_sys_io_submit fs/aio.c:2078 [inline]
__se_sys_io_submit+0x293/0x770 fs/aio.c:2048
__x64_sys_io_submit+0x92/0xd0 fs/aio.c:2048
do_syscall_x64 arch/x86/entry/common.c:50 [inline]
do_syscall_64+0x3d/0xb0 arch/x86/entry/common.c:80
entry_SYSCALL_64_after_hwframe+0x63/0xcd
CPU: 1 PID: 5034 Comm: syz-executor350 Not tainted 6.2.0-rc6-syzkaller-80422-geda666ff2276 #0
Hardware name: Google Google Compute Engine/Google Compute Engine, BIOS Google 01/12/2023
=====================================================
We can follow the call chain and find that 'bcm_tx_setup' function
calls 'memcpy_from_msg' to copy some content to the newly allocated
frame of 'op->frames'. After that the 'len' field of copied structure
being compared with some constant value (64 or 8). However, if
'memcpy_from_msg' returns an error, we will compare some uninitialized
memory. This triggers 'uninit-value' issue.
This patch will add 'memcpy_from_msg' possible errors processing to
avoid uninit-value issue.
Tested via syzkaller |
In the Linux kernel, the following vulnerability has been resolved:
rxrpc: Fix potential data race in rxrpc_wait_to_be_connected()
Inside the loop in rxrpc_wait_to_be_connected() it checks call->error to
see if it should exit the loop without first checking the call state. This
is probably safe as if call->error is set, the call is dead anyway, but we
should probably wait for the call state to have been set to completion
first, lest it cause surprise on the way out.
Fix this by only accessing call->error if the call is complete. We don't
actually need to access the error inside the loop as we'll do that after.
This caused the following report:
BUG: KCSAN: data-race in rxrpc_send_data / rxrpc_set_call_completion
write to 0xffff888159cf3c50 of 4 bytes by task 25673 on cpu 1:
rxrpc_set_call_completion+0x71/0x1c0 net/rxrpc/call_state.c:22
rxrpc_send_data_packet+0xba9/0x1650 net/rxrpc/output.c:479
rxrpc_transmit_one+0x1e/0x130 net/rxrpc/output.c:714
rxrpc_decant_prepared_tx net/rxrpc/call_event.c:326 [inline]
rxrpc_transmit_some_data+0x496/0x600 net/rxrpc/call_event.c:350
rxrpc_input_call_event+0x564/0x1220 net/rxrpc/call_event.c:464
rxrpc_io_thread+0x307/0x1d80 net/rxrpc/io_thread.c:461
kthread+0x1ac/0x1e0 kernel/kthread.c:376
ret_from_fork+0x1f/0x30 arch/x86/entry/entry_64.S:308
read to 0xffff888159cf3c50 of 4 bytes by task 25672 on cpu 0:
rxrpc_send_data+0x29e/0x1950 net/rxrpc/sendmsg.c:296
rxrpc_do_sendmsg+0xb7a/0xc20 net/rxrpc/sendmsg.c:726
rxrpc_sendmsg+0x413/0x520 net/rxrpc/af_rxrpc.c:565
sock_sendmsg_nosec net/socket.c:724 [inline]
sock_sendmsg net/socket.c:747 [inline]
____sys_sendmsg+0x375/0x4c0 net/socket.c:2501
___sys_sendmsg net/socket.c:2555 [inline]
__sys_sendmmsg+0x263/0x500 net/socket.c:2641
__do_sys_sendmmsg net/socket.c:2670 [inline]
__se_sys_sendmmsg net/socket.c:2667 [inline]
__x64_sys_sendmmsg+0x57/0x60 net/socket.c:2667
do_syscall_x64 arch/x86/entry/common.c:50 [inline]
do_syscall_64+0x41/0xc0 arch/x86/entry/common.c:80
entry_SYSCALL_64_after_hwframe+0x63/0xcd
value changed: 0x00000000 -> 0xffffffea |
In the Linux kernel, the following vulnerability has been resolved:
dmaengine: hisilicon: Add multi-thread support for a DMA channel
When we get a DMA channel and try to use it in multiple threads it
will cause oops and hanging the system.
% echo 100 > /sys/module/dmatest/parameters/threads_per_chan
% echo 100 > /sys/module/dmatest/parameters/iterations
% echo 1 > /sys/module/dmatest/parameters/run
[383493.327077] Unable to handle kernel paging request at virtual
address dead000000000108
[383493.335103] Mem abort info:
[383493.335103] ESR = 0x96000044
[383493.335105] EC = 0x25: DABT (current EL), IL = 32 bits
[383493.335107] SET = 0, FnV = 0
[383493.335108] EA = 0, S1PTW = 0
[383493.335109] FSC = 0x04: level 0 translation fault
[383493.335110] Data abort info:
[383493.335111] ISV = 0, ISS = 0x00000044
[383493.364739] CM = 0, WnR = 1
[383493.367793] [dead000000000108] address between user and kernel
address ranges
[383493.375021] Internal error: Oops: 96000044 [#1] PREEMPT SMP
[383493.437574] CPU: 63 PID: 27895 Comm: dma0chan0-copy2 Kdump:
loaded Tainted: GO 5.17.0-rc4+ #2
[383493.457851] pstate: 204000c9 (nzCv daIF +PAN -UAO -TCO -DIT
-SSBS BTYPE=--)
[383493.465331] pc : vchan_tx_submit+0x64/0xa0
[383493.469957] lr : vchan_tx_submit+0x34/0xa0
This occurs because the transmission timed out, and that's due
to data race. Each thread rewrite channels's descriptor as soon as
device_issue_pending is called. It leads to the situation that
the driver thinks that it uses the right descriptor in interrupt
handler while channels's descriptor has been changed by other
thread. The descriptor which in fact reported interrupt will not
be handled any more, as well as its tx->callback.
That's why timeout reports.
With current fixes channels' descriptor changes it's value only
when it has been used. A new descriptor is acquired from
vc->desc_issued queue that is already filled with descriptors
that are ready to be sent. Threads have no direct access to DMA
channel descriptor. In case of channel's descriptor is busy, try
to submit to HW again when a descriptor is completed. In this case,
vc->desc_issued may be empty when hisi_dma_start_transfer is called,
so delete error reporting on this. Now it is just possible to queue
a descriptor for further processing. |
In the Linux kernel, the following vulnerability has been resolved:
nilfs2: do not write dirty data after degenerating to read-only
According to syzbot's report, mark_buffer_dirty() called from
nilfs_segctor_do_construct() outputs a warning with some patterns after
nilfs2 detects metadata corruption and degrades to read-only mode.
After such read-only degeneration, page cache data may be cleared through
nilfs_clear_dirty_page() which may also clear the uptodate flag for their
buffer heads. However, even after the degeneration, log writes are still
performed by unmount processing etc., which causes mark_buffer_dirty() to
be called for buffer heads without the "uptodate" flag and causes the
warning.
Since any writes should not be done to a read-only file system in the
first place, this fixes the warning in mark_buffer_dirty() by letting
nilfs_segctor_do_construct() abort early if in read-only mode.
This also changes the retry check of nilfs_segctor_write_out() to avoid
unnecessary log write retries if it detects -EROFS that
nilfs_segctor_do_construct() returned. |
In the Linux kernel, the following vulnerability has been resolved:
net/mlx5: Handle pairing of E-switch via uplink un/load APIs
In case user switch a device from switchdev mode to legacy mode, mlx5
first unpair the E-switch and afterwards unload the uplink vport.
From the other hand, in case user remove or reload a device, mlx5
first unload the uplink vport and afterwards unpair the E-switch.
The latter is causing a bug[1], hence, handle pairing of E-switch as
part of uplink un/load APIs.
[1]
In case VF_LAG is used, every tc fdb flow is duplicated to the peer
esw. However, the original esw keeps a pointer to this duplicated
flow, not the peer esw.
e.g.: if user create tc fdb flow over esw0, the flow is duplicated
over esw1, in FW/HW, but in SW, esw0 keeps a pointer to the duplicated
flow.
During module unload while a peer tc fdb flow is still offloaded, in
case the first device to be removed is the peer device (esw1 in the
example above), the peer net-dev is destroyed, and so the mlx5e_priv
is memset to 0.
Afterwards, the peer device is trying to unpair himself from the
original device (esw0 in the example above). Unpair API invoke the
original device to clear peer flow from its eswitch (esw0), but the
peer flow, which is stored over the original eswitch (esw0), is
trying to use the peer mlx5e_priv, which is memset to 0 and result in
bellow kernel-oops.
[ 157.964081 ] BUG: unable to handle page fault for address: 000000000002ce60
[ 157.964662 ] #PF: supervisor read access in kernel mode
[ 157.965123 ] #PF: error_code(0x0000) - not-present page
[ 157.965582 ] PGD 0 P4D 0
[ 157.965866 ] Oops: 0000 [#1] SMP
[ 157.967670 ] RIP: 0010:mlx5e_tc_del_fdb_flow+0x48/0x460 [mlx5_core]
[ 157.976164 ] Call Trace:
[ 157.976437 ] <TASK>
[ 157.976690 ] __mlx5e_tc_del_fdb_peer_flow+0xe6/0x100 [mlx5_core]
[ 157.977230 ] mlx5e_tc_clean_fdb_peer_flows+0x67/0x90 [mlx5_core]
[ 157.977767 ] mlx5_esw_offloads_unpair+0x2d/0x1e0 [mlx5_core]
[ 157.984653 ] mlx5_esw_offloads_devcom_event+0xbf/0x130 [mlx5_core]
[ 157.985212 ] mlx5_devcom_send_event+0xa3/0xb0 [mlx5_core]
[ 157.985714 ] esw_offloads_disable+0x5a/0x110 [mlx5_core]
[ 157.986209 ] mlx5_eswitch_disable_locked+0x152/0x170 [mlx5_core]
[ 157.986757 ] mlx5_eswitch_disable+0x51/0x80 [mlx5_core]
[ 157.987248 ] mlx5_unload+0x2a/0xb0 [mlx5_core]
[ 157.987678 ] mlx5_uninit_one+0x5f/0xd0 [mlx5_core]
[ 157.988127 ] remove_one+0x64/0xe0 [mlx5_core]
[ 157.988549 ] pci_device_remove+0x31/0xa0
[ 157.988933 ] device_release_driver_internal+0x18f/0x1f0
[ 157.989402 ] driver_detach+0x3f/0x80
[ 157.989754 ] bus_remove_driver+0x70/0xf0
[ 157.990129 ] pci_unregister_driver+0x34/0x90
[ 157.990537 ] mlx5_cleanup+0xc/0x1c [mlx5_core]
[ 157.990972 ] __x64_sys_delete_module+0x15a/0x250
[ 157.991398 ] ? exit_to_user_mode_prepare+0xea/0x110
[ 157.991840 ] do_syscall_64+0x3d/0x90
[ 157.992198 ] entry_SYSCALL_64_after_hwframe+0x46/0xb0 |
In the Linux kernel, the following vulnerability has been resolved:
media: ov2740: Fix memleak in ov2740_init_controls()
There is a kmemleak when testing the media/i2c/ov2740.c with bpf mock
device:
unreferenced object 0xffff8881090e19e0 (size 16):
comm "51-i2c-ov2740", pid 278, jiffies 4294781584 (age 23.613s)
hex dump (first 16 bytes):
00 f3 7c 0b 81 88 ff ff 80 75 6a 09 81 88 ff ff ..|......uj.....
backtrace:
[<000000004e9fad8f>] __kmalloc_node+0x44/0x1b0
[<0000000039c802f4>] kvmalloc_node+0x34/0x180
[<000000009b8b5c63>] v4l2_ctrl_handler_init_class+0x11d/0x180
[videodev]
[<0000000038644056>] ov2740_probe+0x37d/0x84f [ov2740]
[<0000000092489f59>] i2c_device_probe+0x28d/0x680
[<000000001038babe>] really_probe+0x17c/0x3f0
[<0000000098c7af1c>] __driver_probe_device+0xe3/0x170
[<00000000e1b3dc24>] device_driver_attach+0x34/0x80
[<000000005a04a34d>] bind_store+0x10b/0x1a0
[<00000000ce25d4f2>] drv_attr_store+0x49/0x70
[<000000007d9f4e9a>] sysfs_kf_write+0x8c/0xb0
[<00000000be6cff0f>] kernfs_fop_write_iter+0x216/0x2e0
[<0000000031ddb40a>] vfs_write+0x658/0x810
[<0000000041beecdd>] ksys_write+0xd6/0x1b0
[<0000000023755840>] do_syscall_64+0x38/0x90
[<00000000b2cc2da2>] entry_SYSCALL_64_after_hwframe+0x63/0xcd
ov2740_init_controls() won't clean all the allocated resources in fail
path, which may causes the memleaks. Add v4l2_ctrl_handler_free() to
prevent memleak. |
In the Linux kernel, the following vulnerability has been resolved:
bus: fsl-mc: don't assume child devices are all fsl-mc devices
Changes in VFIO caused a pseudo-device to be created as child of
fsl-mc devices causing a crash [1] when trying to bind a fsl-mc
device to VFIO. Fix this by checking the device type when enumerating
fsl-mc child devices.
[1]
Modules linked in:
Internal error: Oops: 0000000096000004 [#1] PREEMPT SMP
CPU: 6 PID: 1289 Comm: sh Not tainted 6.2.0-rc5-00047-g7c46948a6e9c #2
Hardware name: NXP Layerscape LX2160ARDB (DT)
pstate: 60000005 (nZCv daif -PAN -UAO -TCO -DIT -SSBS BTYPE=--)
pc : mc_send_command+0x24/0x1f0
lr : dprc_get_obj_region+0xfc/0x1c0
sp : ffff80000a88b900
x29: ffff80000a88b900 x28: ffff48a9429e1400 x27: 00000000000002b2
x26: ffff48a9429e1718 x25: 0000000000000000 x24: 0000000000000000
x23: ffffd59331ba3918 x22: ffffd59331ba3000 x21: 0000000000000000
x20: ffff80000a88b9b8 x19: 0000000000000000 x18: 0000000000000001
x17: 7270642f636d2d6c x16: 73662e3030303030 x15: ffffffffffffffff
x14: ffffd59330f1d668 x13: ffff48a8727dc389 x12: ffff48a8727dc386
x11: 0000000000000002 x10: 00008ceaf02f35d4 x9 : 0000000000000012
x8 : 0000000000000000 x7 : 0000000000000006 x6 : ffff80000a88bab0
x5 : 0000000000000000 x4 : 0000000000000000 x3 : ffff80000a88b9e8
x2 : ffff80000a88b9e8 x1 : 0000000000000000 x0 : ffff48a945142b80
Call trace:
mc_send_command+0x24/0x1f0
dprc_get_obj_region+0xfc/0x1c0
fsl_mc_device_add+0x340/0x590
fsl_mc_obj_device_add+0xd0/0xf8
dprc_scan_objects+0x1c4/0x340
dprc_scan_container+0x38/0x60
vfio_fsl_mc_probe+0x9c/0xf8
fsl_mc_driver_probe+0x24/0x70
really_probe+0xbc/0x2a8
__driver_probe_device+0x78/0xe0
device_driver_attach+0x30/0x68
bind_store+0xa8/0x130
drv_attr_store+0x24/0x38
sysfs_kf_write+0x44/0x60
kernfs_fop_write_iter+0x128/0x1b8
vfs_write+0x334/0x448
ksys_write+0x68/0xf0
__arm64_sys_write+0x1c/0x28
invoke_syscall+0x44/0x108
el0_svc_common.constprop.1+0x94/0xf8
do_el0_svc+0x38/0xb0
el0_svc+0x20/0x50
el0t_64_sync_handler+0x98/0xc0
el0t_64_sync+0x174/0x178
Code: aa0103f4 a9025bf5 d5384100 b9400801 (79401260)
---[ end trace 0000000000000000 ]--- |
In the Linux kernel, the following vulnerability has been resolved:
ip6mr: Fix skb_under_panic in ip6mr_cache_report()
skbuff: skb_under_panic: text:ffffffff88771f69 len:56 put:-4
head:ffff88805f86a800 data:ffff887f5f86a850 tail:0x88 end:0x2c0 dev:pim6reg
------------[ cut here ]------------
kernel BUG at net/core/skbuff.c:192!
invalid opcode: 0000 [#1] PREEMPT SMP KASAN
CPU: 2 PID: 22968 Comm: kworker/2:11 Not tainted 6.5.0-rc3-00044-g0a8db05b571a #236
Hardware name: QEMU Standard PC (i440FX + PIIX, 1996), BIOS 1.15.0-1 04/01/2014
Workqueue: ipv6_addrconf addrconf_dad_work
RIP: 0010:skb_panic+0x152/0x1d0
Call Trace:
<TASK>
skb_push+0xc4/0xe0
ip6mr_cache_report+0xd69/0x19b0
reg_vif_xmit+0x406/0x690
dev_hard_start_xmit+0x17e/0x6e0
__dev_queue_xmit+0x2d6a/0x3d20
vlan_dev_hard_start_xmit+0x3ab/0x5c0
dev_hard_start_xmit+0x17e/0x6e0
__dev_queue_xmit+0x2d6a/0x3d20
neigh_connected_output+0x3ed/0x570
ip6_finish_output2+0x5b5/0x1950
ip6_finish_output+0x693/0x11c0
ip6_output+0x24b/0x880
NF_HOOK.constprop.0+0xfd/0x530
ndisc_send_skb+0x9db/0x1400
ndisc_send_rs+0x12a/0x6c0
addrconf_dad_completed+0x3c9/0xea0
addrconf_dad_work+0x849/0x1420
process_one_work+0xa22/0x16e0
worker_thread+0x679/0x10c0
ret_from_fork+0x28/0x60
ret_from_fork_asm+0x11/0x20
When setup a vlan device on dev pim6reg, DAD ns packet may sent on reg_vif_xmit().
reg_vif_xmit()
ip6mr_cache_report()
skb_push(skb, -skb_network_offset(pkt));//skb_network_offset(pkt) is 4
And skb_push declared as:
void *skb_push(struct sk_buff *skb, unsigned int len);
skb->data -= len;
//0xffff88805f86a84c - 0xfffffffc = 0xffff887f5f86a850
skb->data is set to 0xffff887f5f86a850, which is invalid mem addr, lead to skb_push() fails. |
A vulnerability has been found in SourceCodester Online Student File Management System 1.0. Affected by this issue is some unknown functionality of the file /admin/delete_user.php. The manipulation of the argument user_id leads to sql injection. The attack can be initiated remotely. The exploit has been disclosed to the public and may be used. |
In the Linux kernel, the following vulnerability has been resolved:
skmsg: pass gfp argument to alloc_sk_msg()
syzbot found that alloc_sk_msg() could be called from a
non sleepable context. sk_psock_verdict_recv() uses
rcu_read_lock() protection.
We need the callers to pass a gfp_t argument to avoid issues.
syzbot report was:
BUG: sleeping function called from invalid context at include/linux/sched/mm.h:274
in_atomic(): 0, irqs_disabled(): 0, non_block: 0, pid: 3613, name: syz-executor414
preempt_count: 0, expected: 0
RCU nest depth: 1, expected: 0
INFO: lockdep is turned off.
CPU: 0 PID: 3613 Comm: syz-executor414 Not tainted 6.0.0-syzkaller-09589-g55be6084c8e0 #0
Hardware name: Google Google Compute Engine/Google Compute Engine, BIOS Google 09/22/2022
Call Trace:
<TASK>
__dump_stack lib/dump_stack.c:88 [inline]
dump_stack_lvl+0x1e3/0x2cb lib/dump_stack.c:106
__might_resched+0x538/0x6a0 kernel/sched/core.c:9877
might_alloc include/linux/sched/mm.h:274 [inline]
slab_pre_alloc_hook mm/slab.h:700 [inline]
slab_alloc_node mm/slub.c:3162 [inline]
slab_alloc mm/slub.c:3256 [inline]
kmem_cache_alloc_trace+0x59/0x310 mm/slub.c:3287
kmalloc include/linux/slab.h:600 [inline]
kzalloc include/linux/slab.h:733 [inline]
alloc_sk_msg net/core/skmsg.c:507 [inline]
sk_psock_skb_ingress_self+0x5c/0x330 net/core/skmsg.c:600
sk_psock_verdict_apply+0x395/0x440 net/core/skmsg.c:1014
sk_psock_verdict_recv+0x34d/0x560 net/core/skmsg.c:1201
tcp_read_skb+0x4a1/0x790 net/ipv4/tcp.c:1770
tcp_rcv_established+0x129d/0x1a10 net/ipv4/tcp_input.c:5971
tcp_v4_do_rcv+0x479/0xac0 net/ipv4/tcp_ipv4.c:1681
sk_backlog_rcv include/net/sock.h:1109 [inline]
__release_sock+0x1d8/0x4c0 net/core/sock.c:2906
release_sock+0x5d/0x1c0 net/core/sock.c:3462
tcp_sendmsg+0x36/0x40 net/ipv4/tcp.c:1483
sock_sendmsg_nosec net/socket.c:714 [inline]
sock_sendmsg net/socket.c:734 [inline]
__sys_sendto+0x46d/0x5f0 net/socket.c:2117
__do_sys_sendto net/socket.c:2129 [inline]
__se_sys_sendto net/socket.c:2125 [inline]
__x64_sys_sendto+0xda/0xf0 net/socket.c:2125
do_syscall_x64 arch/x86/entry/common.c:50 [inline]
do_syscall_64+0x2b/0x70 arch/x86/entry/common.c:80
entry_SYSCALL_64_after_hwframe+0x63/0xcd |
In the Linux kernel, the following vulnerability has been resolved:
i2c: designware: Fix handling of real but unexpected device interrupts
Commit c7b79a752871 ("mfd: intel-lpss: Add Intel Alder Lake PCH-S PCI
IDs") caused a regression on certain Gigabyte motherboards for Intel
Alder Lake-S where system crashes to NULL pointer dereference in
i2c_dw_xfer_msg() when system resumes from S3 sleep state ("deep").
I was able to debug the issue on Gigabyte Z690 AORUS ELITE and made
following notes:
- Issue happens when resuming from S3 but not when resuming from
"s2idle"
- PCI device 00:15.0 == i2c_designware.0 is already in D0 state when
system enters into pci_pm_resume_noirq() while all other i2c_designware
PCI devices are in D3. Devices were runtime suspended and in D3 prior
entering into suspend
- Interrupt comes after pci_pm_resume_noirq() when device interrupts are
re-enabled
- According to register dump the interrupt really comes from the
i2c_designware.0. Controller is enabled, I2C target address register
points to a one detectable I2C device address 0x60 and the
DW_IC_RAW_INTR_STAT register START_DET, STOP_DET, ACTIVITY and
TX_EMPTY bits are set indicating completed I2C transaction.
My guess is that the firmware uses this controller to communicate with
an on-board I2C device during resume but does not disable the controller
before giving control to an operating system.
I was told the UEFI update fixes this but never the less it revealed the
driver is not ready to handle TX_EMPTY (or RX_FULL) interrupt when device
is supposed to be idle and state variables are not set (especially the
dev->msgs pointer which may point to NULL or stale old data).
Introduce a new software status flag STATUS_ACTIVE indicating when the
controller is active in driver point of view. Now treat all interrupts
that occur when is not set as unexpected and mask all interrupts from
the controller. |
In the Linux kernel, the following vulnerability has been resolved:
drm/ttm: check null pointer before accessing when swapping
Add a check to avoid null pointer dereference as below:
[ 90.002283] general protection fault, probably for non-canonical
address 0xdffffc0000000000: 0000 [#1] PREEMPT SMP KASAN NOPTI
[ 90.002292] KASAN: null-ptr-deref in range
[0x0000000000000000-0x0000000000000007]
[ 90.002346] ? exc_general_protection+0x159/0x240
[ 90.002352] ? asm_exc_general_protection+0x26/0x30
[ 90.002357] ? ttm_bo_evict_swapout_allowable+0x322/0x5e0 [ttm]
[ 90.002365] ? ttm_bo_evict_swapout_allowable+0x42e/0x5e0 [ttm]
[ 90.002373] ttm_bo_swapout+0x134/0x7f0 [ttm]
[ 90.002383] ? __pfx_ttm_bo_swapout+0x10/0x10 [ttm]
[ 90.002391] ? lock_acquire+0x44d/0x4f0
[ 90.002398] ? ttm_device_swapout+0xa5/0x260 [ttm]
[ 90.002412] ? lock_acquired+0x355/0xa00
[ 90.002416] ? do_raw_spin_trylock+0xb6/0x190
[ 90.002421] ? __pfx_lock_acquired+0x10/0x10
[ 90.002426] ? ttm_global_swapout+0x25/0x210 [ttm]
[ 90.002442] ttm_device_swapout+0x198/0x260 [ttm]
[ 90.002456] ? __pfx_ttm_device_swapout+0x10/0x10 [ttm]
[ 90.002472] ttm_global_swapout+0x75/0x210 [ttm]
[ 90.002486] ttm_tt_populate+0x187/0x3f0 [ttm]
[ 90.002501] ttm_bo_handle_move_mem+0x437/0x590 [ttm]
[ 90.002517] ttm_bo_validate+0x275/0x430 [ttm]
[ 90.002530] ? __pfx_ttm_bo_validate+0x10/0x10 [ttm]
[ 90.002544] ? kasan_save_stack+0x33/0x60
[ 90.002550] ? kasan_set_track+0x25/0x30
[ 90.002554] ? __kasan_kmalloc+0x8f/0xa0
[ 90.002558] ? amdgpu_gtt_mgr_new+0x81/0x420 [amdgpu]
[ 90.003023] ? ttm_resource_alloc+0xf6/0x220 [ttm]
[ 90.003038] amdgpu_bo_pin_restricted+0x2dd/0x8b0 [amdgpu]
[ 90.003210] ? __x64_sys_ioctl+0x131/0x1a0
[ 90.003210] ? do_syscall_64+0x60/0x90 |
In the Linux kernel, the following vulnerability has been resolved:
PCI: Fix use-after-free in pci_bus_release_domain_nr()
Commit c14f7ccc9f5d ("PCI: Assign PCI domain IDs by ida_alloc()")
introduced a use-after-free bug in the bus removal cleanup. The issue was
found with kfence:
[ 19.293351] BUG: KFENCE: use-after-free read in pci_bus_release_domain_nr+0x10/0x70
[ 19.302817] Use-after-free read at 0x000000007f3b80eb (in kfence-#115):
[ 19.309677] pci_bus_release_domain_nr+0x10/0x70
[ 19.309691] dw_pcie_host_deinit+0x28/0x78
[ 19.309702] tegra_pcie_deinit_controller+0x1c/0x38 [pcie_tegra194]
[ 19.309734] tegra_pcie_dw_probe+0x648/0xb28 [pcie_tegra194]
[ 19.309752] platform_probe+0x90/0xd8
...
[ 19.311457] kfence-#115: 0x00000000063a155a-0x00000000ba698da8, size=1072, cache=kmalloc-2k
[ 19.311469] allocated by task 96 on cpu 10 at 19.279323s:
[ 19.311562] __kmem_cache_alloc_node+0x260/0x278
[ 19.311571] kmalloc_trace+0x24/0x30
[ 19.311580] pci_alloc_bus+0x24/0xa0
[ 19.311590] pci_register_host_bridge+0x48/0x4b8
[ 19.311601] pci_scan_root_bus_bridge+0xc0/0xe8
[ 19.311613] pci_host_probe+0x18/0xc0
[ 19.311623] dw_pcie_host_init+0x2c0/0x568
[ 19.311630] tegra_pcie_dw_probe+0x610/0xb28 [pcie_tegra194]
[ 19.311647] platform_probe+0x90/0xd8
...
[ 19.311782] freed by task 96 on cpu 10 at 19.285833s:
[ 19.311799] release_pcibus_dev+0x30/0x40
[ 19.311808] device_release+0x30/0x90
[ 19.311814] kobject_put+0xa8/0x120
[ 19.311832] device_unregister+0x20/0x30
[ 19.311839] pci_remove_bus+0x78/0x88
[ 19.311850] pci_remove_root_bus+0x5c/0x98
[ 19.311860] dw_pcie_host_deinit+0x28/0x78
[ 19.311866] tegra_pcie_deinit_controller+0x1c/0x38 [pcie_tegra194]
[ 19.311883] tegra_pcie_dw_probe+0x648/0xb28 [pcie_tegra194]
[ 19.311900] platform_probe+0x90/0xd8
...
[ 19.313579] CPU: 10 PID: 96 Comm: kworker/u24:2 Not tainted 6.2.0 #4
[ 19.320171] Hardware name: /, BIOS 1.0-d7fb19b 08/10/2022
[ 19.325852] Workqueue: events_unbound deferred_probe_work_func
The stack trace is a bit misleading as dw_pcie_host_deinit() doesn't
directly call pci_bus_release_domain_nr(). The issue turns out to be in
pci_remove_root_bus() which first calls pci_remove_bus() which frees the
struct pci_bus when its struct device is released. Then
pci_bus_release_domain_nr() is called and accesses the freed struct
pci_bus. Reordering these fixes the issue. |